Sweating the 45… (Part4)

Last week I looked at optimising  the 45 loadline in A2.  Clearly we shouldn’t be attempting to get more than 2W from this valve without a significant level of distortion. However, having about of 3W would be attractive for the transient response of this amp.

So how will this circuit perform in a simulation? Let’s see what the spice results are:

45 SE A2 amp version 02The THD is significantly better due to the harmonic cancellation between the two stages. The driver distortion is  0.3% at full tilt (150vpp) and this could be improved. I guess the 6e5p could do better, but interesting to see how the cancellation of harmonics may play around. The new operating point and the stacked supplies will demand different MOSFET parts of 1kV for sure…

 

45 SE Amplifier upgrade

Replacing driver for 7193 valve

Well, after nearly 12 months of playing relentlessly my 45 SE amplifier, had an unexpected failure in the power supply (passive regulator) which forced me to do maintenance to the amplifier. It was a great opportunity to remove the 6J5 driver and do a quick swap for the greatly respected 7193 (i.e. military version of the 2c22)

45SE Amplifier upgraded with the 7193 drivers

Bias point remains unchanged: 7mA and 260V for maximum swing and minimum distortion. Need to look at my notes, but I remember that I was something around 0.30% at 100Vpp driving the 45 (which is not an easy load for anyone).  Driver configuration was not changed, so had the 7193 now loaded with same DN2540 single transistor gyrator and mu-follower output for lower impedance. The valve was biased at about 8V with an LED array.

7193 in action

As a test, played the fantastic Symphony No. 3 from Henryk Gorecki….