811a SE Amplifier with a twist

Goodbye Jon

Sadly, yesterday heard the sad news that our friend Jon Finlayson from the London Audio Circle passed away.  Jon was an incredible person, a true music lover and passionate about life. He introduced me to most of the circle team members and enjoyed thoroughly the meeting at his place and listen to his electrostatic speakers and constantly evolving system.

I learnt such a great deal of stuff from him and will remember our conversations and how passionate and meticulous he was into doing things. In particular when I built my Starlight CD player and he helped me out with the DAC ladder resistor matching.

See you on the other side Jon.

The 811a amplifier

The last year of the pandemic allowed me to do some experiments whilst being more at home. I hooked up an 811a on the bench with the following circuit:

I reused my original D3a driver from the 300B SE Amplifier. That was an easy choice and speed up my building process. I added a PMOS driver for a “plate to grid” feedback. The feedback network was somehow tricky to trim as had limited resistors available but the combination of 2 39KΩ resistors and a 18KΩ resistor worked well. The follower helped with driving the positive grid current which is about 16mA on idle at 22.5V bias or so. The bias is actually adjusted with a positive regulator set to about 50V on the PMOS gate.

I ended up building a PCB for the PMOS driver, very simple but effective.  I used an SMPS for the filament supply and was good enough for testing purposes.

The iron was some Lundahl gapped at 90mA which I had at hand, but can be anything you want.

Power? Oh yes, could extract 16W at about 1.5% and think measured 18W before clipping.  Distortion at low power (e.g. 2W) was less than 0.4% so a nice beauty to listen to. I love the sound I got out of it, not my normal listening system and couldn’t move the whole Frankenstein down to where my speakers are with the kids around and 600V all over it (long are gone those days where 600V were everywhere in my music cabinet).

 

 

“Schade” SE Amp Example

Introduction

On my last post I covered how the gyrator PCB can be used in a pentode driver. The pentode driver is the best candidate in a “plate to plate” / shunt feedback or “Schade” feedback amplifier which is the name typically used in the DIYAudio world. The triode doesn’t work well here as you need high gain and low distortion with a load which can get quite low (due to the feedback effect of the feedback resistor). I’m not going to cover the subject as it has been covered (and discussed) extensively before by many people, so I suggest you do a bit of research yourself if you are interested in the subject and want to learn more. 

A Study example

Continue reading ““Schade” SE Amp Example”

Robustiano (V0.7)

Hacked a simple PCB to build the follower to drive the 4P1L as suggested by Rod. I had to play with the LND150 setting resistor (R4) to achieve the 2mA of idle current. I ended up biasing the 4P1L rather hot at about 11.5W which exceeds the specs. The Q2 VBE was not possible to measure as the Q2 would oscillate I guess when I place the tester lead on Q1 collector and the voltage seems to drop when I try to measure it. Should have added a ferrite bead:

Robustiano v07 bench test

When measuring distortion against frequency, I was keen to see that the follower provided some impact in reducing the HF distortion. For example at 20kHz, THD reduced from 0.96% to 0.59% @1W output power and from 7.84% to  3.52%, that is close to half the distortion I had before:

Robustiano v07 THD tests

What is nice to see now is the effect of the follower providing sufficient source current to the 4P1L grid. Above 2.5W, the grid current kicks in and we can see how “Robustiano” can deliver 3W at less than 1% until starts to clip about 3.5W:

Robustiano v07 THD versus power

I found that if I were to reduce the Rf further and therefore increasing the collector current but obviously exceeding the 4P1L power dissipation too much as collector current was about 45-48mA, the distortion at 20kHz falls significantly. I suspect I should increase the collector current to enable better drive of Q2 due to its Cib (30pF). To keep the current feedback arrangement this could be done by reducing the negative emitter voltage source (V1). Should try this I guess…

20140726-093332-34412311.jpg

 

Cheers

Ale

Robustiano (version 0.6)

It was now the turn to the BJT to show what it can do in this circuit. Here is my quick breadboard with components I had at hand, so there is a slight variation from the simulation:

Robustiano 4P1L v06 BJT testThe Q1 is obviously an MPSA42. C3 was substituted with a 10uF/25V electrolytic (yes you read well). Rf is a 250k carbon pot and R2 is built of a series of 1K pair in parallel plus 100 ohms in parallel, four resistors are wire-wound 1W. C1 is actually a 30uF/450V ASC Oil cap.

I haven’t measured the collector current but it seems to be around 1.3-18mA. Variance is due to tolerance of RE and R3. I need to measure the actual resistance of Rf but is somewhere between 180 and 200K.

As Rod suggested, the circuit is very stable and easy to dial the right feedback with the potentiometer. The 4P1L is biased about -9V and is slightly under the max Pa in this case.

Distortion is as predicted in the simulation (e.g. 0.1% for 1W and about 0.2 – 0.25% for 2W). Just above 2.2W distortion creeps up rapidly given grid current, which is not modelled properly by the 4P1L pentode model:

Robustiano v06 THD versus powerLooking at distortion versus frequency, it’s interesting to compare the BJT performance against the depletion FET. With lower Cob compared to the Coss of the FET, the BJT should be able to drive better the 4P1L. In fact, the BJT is more linear when swinging many volts compared to the depletion FET, so the proof is in the pudding:

Robustiano v06 tests THD The BJT is indeed more linear but if we compare the THD vs frequency of both drivers when providing 2W output power, we can see that the BJT is suffering as much (and even more given poorer slew rate) than the FET at frequencies above 12kHz. Also FET’s THD versus frequency is more linear up to 10kHz, whereas the BJT has a peak around 6kHz and a dip closer to 10-11kHz. Either way, the BJT outperforms the FET in overall THD up to 11kHz.

I need to listen to this circuit now…

 

 

Robustiano (Version 0.4)

Finally back home after a long trip and had the opportunity to put the DN2540 at test and try the topologies discussed for the “Schade” feedback 4P1L SE amplifier. So I re-build my test rig and tried the DN2540 and LND150 at various drain currents. It was clearly to see that in order to keep distortion to a minimum, the VDS needs to be greater than 60V to keep the output capacitance of the FET low. Here are the results of the frequency response at nearly maximum output power (Po=2W):

Robustiano 4P1L VER 0.4 DRIVER TESTSIt is interesting to see that the LND150 which has Coss (max) of 3.5pF doesn’t perform much better than the DN2540 which has Coss (max) of about 30pF. Operating points are different for both FETs but the 4P1L is running about the same operating conditions. What is also interesting to verify with this test is that the higher the drain current, the more capability the FET has to drive the 4P1L input (and Coss) capacitance at higher frequencies as the slew rate of the FET is higher.

ROBUSTIANO 4P1L VER04 THD VS POWER

We can see an interesting improvement from my initial tests at 5mA when drain current was just about 1.5mA. The yellow trace (Id=5mA) shows the best performance of the DN2540. Surely higher drain current will perform better but at a cost as the drain current is part of the OT primary current.

So how do we keep the gain of the FET when increasing the drain current? The natural approach will be to reduce Rf, but this affects the FET gain and the feedback. The alternative is to increase the supply voltage respect to ground. The price we pay here is to increase the cathode resistor and burning the power on it. With -4V as the negative source supply voltage, I had to only reduce RF to 51.5K to set 5mA on the DN2540. The supply power was increased to 350V, the screen (Vg2k) to about 140V (240-98.6V) which is lower than the 150V used before. There is a tad of extra power to extract on the 4P1L but here is close to its maximum dissipation. The Rk is a pair of wirewound 4K7 in parallel.

Robustiano 4P1L SE Schade v01.

 

 

 

 

 

 

 

 

 

 

 

I think it is now time to try the BJT driver. I suspect that it will need at least 5mA of collector current to get on with the task of the input capacitance of the 4P1L when anode to grid feedback is in place.

cheers

Ale

 

 

2e24 DHT

IMG_0369 SMALL It was suggested to me recently by Piotr to explore the 2e24 after looking at the 2e22. This small directly heated pentode have about 10-12W of anode dissipation depending how it’s wired. I suspected this DHT in triode mode will have a high anode resistance so as soon as I managed to get hold of a sample, I submitted it to the mercy of my curve tracer:

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307a DHT in triode and Schade feedback

IMG_0339Vegard Winge kindly sent me some great DHTs for tracing including the 307a directly heated pentode. The sample traced is not an original Western Electric but a lovely Raytheon RK 75 307a NOS. There is limited information of this valve in triode mode and the folks at DIYaudio are looking at potentially using it for a DHT headphone amp.

This valve has a filament of 5.5V and 1A and an anode dissipation of 21W in class A (including screen dissipation) when triode-connected.

Let’s see how this valve performs in triode-mode:

307a triodeSMALL

 

 

How well can we match a triode model for this valve?

307a triode small

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