6e6p-dr HP amp – part 3: measurements

As I promised, I took the HP amp back to the workshop for a bit of abuse on the bench. Here are some interesting measurements which correlate with some of my listening impressions so far.

I added a set of 300Ω dummy loads at the output to simulate the HPs. Firstly I tested the optimal circuit which has the Sowter 8665 output transformer in Parafeed mode (4:1) to drive the load. You can get a very clean and flat response across the audio band from 3Hz up to +90kHz. There is a minor hump to be tuned due to the RLC circuit formed by the parafeed circuit. I used a 4.7μF Mundorf EVO oil cap. It’s pretty flat to me, so will leave it there.

The performance of the circuit is amazing. Distortion is very low, up to 0.07% at 100mW (which is VL=5.47Vrms):

6e6p-dr Headphone Amp performance @ 100mW output level
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6e6p-dr Headphone Amp – part 3

6e6p-dr HP amp in action – cap coupled output

I’ve been running with this HP amplifier for a few weeks now and I have to say I’m delighted with it. I matched a pair of 6e6p-dr on my eTracer and after fiddling with the operating point a bit, I settled for Ia=25mA and Va=180V. Anode voltage will depend on the valve as said before, the Russian valve parameters tend to be all over the place. Anyhow, expect anode voltage to be around 170 to 185V. The beauty of the gyrator PCB is that you can adjust the anode voltage with the trimpot.

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HP experiments – part 1

Experimenting on headphone amplifiers, not always turn out the way you expected. Well, that’s the nature of experimentation and some smoke may come along the way.

Here is my new take on the headphone amp. Modified the 2P29L to fit the 6e6p-dr valve. I love this IHT one, so wanted to experiment more.

Instead of the classic HT, I used some Chinese 300-450V SMPS modules. I used the 70W version with success before, not these tiny ones.

Individually tested all parts and worked fine. Fired up the SMPS with the hot filaments and the 6e6p-dr running at 20mA each and the SMPS oscillated. They went to 450V instead of the 250V dialled and one of my cap multiplier PCB boards got damaged. Damn!

Back to the drawing board. I will probably stick to the simple HT supply 🙂